Pratik Sunil Raut
Department of Textile Technology
Shri Guru Gobind Singhji Institute of
Engineering and Technology, (SGGS I E&T ), Vishnupuri,Nanded, (Maharashtra
State, India)
Abstract
In key concern for any of the owner in textile industry is production. This always attracted machines manufacturers and researchers to make
new developments in machines and processes. Air-jet is one of the successful highest productive weaving machines. However, it is now well
established that due to add of charges of compressed air, manufacturing cost of fabric on air-jet weaving machine is higher as compared with rapier and projectile
weaving machines. Countries those who are having energy issues majorly does not prefer
air-jet weaving machines. Manufacturer's
continuously been working on the reduction of air consumption . In this study, we aim to investigate the possibilities to reduce air consumption on
current air-jet weaving looms without making a new investment in a weaving
mill. Decrease of air consumption by 21% was achieved in a weaving mill
by decreasing the hole diameter of the single-holed relay nozzles and by
optimizing the blowing time of the multi-holed relay nozzles.Thus, a company
having 202 looms could save 240,000 € per year in electricity costs with almost
no expense.This paper elaborates the experimental work which was conducted in the weaving
mill in order to reduce air consumption on air-jet looms.
Keywords: Air jet loom,Compressed
air consumption,hole diameter of single relay nozzle, blowing time of
multi-holed relay nozzle, production
INTRODUCTION
Air-Jet weaving machine is one of the successful and high
productive shuttle less weaving machine in Textile industry . Air-jet is
device which is used to insert the weft yarn by using high air pressure on the air jet loom. The air is
filtered and compressed before using on loom. Because of the significant
compressed air consumption and additional cost of compressor electricity, the
manufacturing cost of air- jet weaving is high as compare with the other weaving systems. This is the reason which is making air-jet
weaving less preferable where energy cost is the problem despite their high
production speed rates. For the same reason air-jet weaving machines manufacturers and researchers
have been continuously working on reduction of air consumption in their new
design to overcome this drawback. Thus this study aims to significantly to reduce air
consumption by optimizing some loom parameters in a weaving mill. It is mainly
focused on relay nozzles due to the fact that 80% of compressed air is consumed
by these nozzles.
Literature reviews
For decades, scores of textile researchers and machine
manufactures attempt to develop the construction of air jet weaving
machine as it is very popular in the weaving industries because of its higher
productivity and capable of texturing spun and cellulose filament fabrics which
could not be produced by other looms [9]. Money-spinning air jet loom is vastly
recommended by the producer as textile is a power exhaustive sector. So many
articles are published on the theme of air jet loom productivity, air
consumption, setting points, history, and sequential development in the
construction. Few literary documents on this topic are enlisted in our article.
Pioneer Adanur
published his valuable research text such as he pointed out that
the air jet weaving machines belong to the set of interermittent-operation of
loom [10]. He also mentioned that the air pressure from the central air tank to
the loom cnverted into kinetic energy in the nozzle, which push weft in the air
channels differently shaped by loom types . By maintaining the air pressure of
the air jet loom along the main valve & relay valve drive time low air will
be consumed without hampering product quality . Poppe studied the air index and
claimed that air consumption decreased as the yarn hairiness increased
.Tarabadkar indicated the importance of compressors on air consumption in
spinning and weaving machines . Many researchers studied the various loom parts
such as the nozzle, reed, and valves in order to improve the filling rates and to decrease air consumption and thus they invented an optimum main nozzle design. Scientists like Mohamed and Salama had studied the mechanics of the air-jet filling rates and
the nozzle design . Picanol had developed air-index as a measure of weft yarn majorly necessity for air-jet weaving had also led to the development of a new relay nozzle design with
16 holes in order to reduce air consumption . Dornier had developed a PIC (Permanent Insertion
Control) system for permanent monitoring of the most important filling
insertion elements. In the similar way, Sultex claims an outstanding results with regards to the compressed air consumption on L-5500 looms withn new AWC (Active Weft
Control) system . Many other loom makers also claims a great reductions in air
consumption following new developments in their designs. Özer Göktepe and Orcun
Bozkan showed that weaving mills could obtain considerable savings in energy
costs by working with single-holed relay nozzles having smaller hole diameter
and by achieving the shortest possible blowing time adjustments on air-jet
looms equipped with multi-holed relay nozzles, without any decrease in loom
efficiency and performance . Islam M.M., Hanifa A.M.A. showed that using low air
pressure air consumption and cost of air-jet loom can be reduced . Raj Kumar
Khiani suggested some measures in his paper to reduce the air consumption in
air-jet loom . Even if air-jet weaving machines manufacturers and researchers
have been continuously working on reduction of air consumption in their new
design to overcome the negative aspect of high consumption of air and
additional cost of compressor electricity until now there is still deficiency
of reliable information on energy efficiency of compressed air for
industries
Experimental details
This study was conducted in a large-scale weaving mill
having a total of 202 air-jet looms (75 of the looms were Dornier
LW, model 1997, while 127 of them were Picanol Omni Plus, model 2000). Dornier
looms were equipped with single -holed relay nozzles while Picanol looms were
equipped with multi-holed relay nozzles. The main aim was to minimize the air
consumption by optimizing some parameters of the relay nozzles and the selvedge
pattern. For this purpose, the effect of relay nozzle diameter, relay nozzle
blowing time, number of holes on the relay nozzles, anbeen changed by the
weavers until this study. Experiments regarding relay nozzle diameter and
selvedge pattern were conducted on the Dornier looms while optimization of
blowing times and number of holes on the relay nozzles were carried out on the
Picanol looms. In calculation of the total energy saving, one day was assumed
to be 24 hours and a year was assumed to be 365 days since all the machines were
running on a 24 hour–365 day basis in the mill. In order investigate the
effect of relay nozzle diameter,two of
the Dornier LW air-jet weaving machines were used.
Both looms weaved the same fabric with the same working parameters
except for the relay nozzle diameters, as shown in Table 1. The first loom was
equipped with relay nozzles with a single hole of 1.4 mm diameter while the
second one was equipped with relay nozzles with a single hole of 1.0 mm
diameter (Figure 4). In total, 24 measurements of air consumption were taken by
a scaled flow meter on both weaving machines for a two-month period n the
second part of the work, blowing times of relay nozzles were optimized on the
Picanol Omni Plus looms.D etails of the loom and fabric woven in this part of
the experimental work are also given in Table 1. The looms were equipped with
the relay nozzles having 19 holes. For optimization, the blowing time of the
relay nozzles was reduced dramatically first, then increased periodically at 4-
day intervals for fine-tuning to determine the minimum blowing time that
enables a problem-free weaving process.
Then the average increase in air consumption with blowing time was
measured to calculate the reduction in total air cosumption obtained by
decreasing the blowing times of the relay nozzles. Aftter optimization of
blowing times, the conventional nozzles having 19 holes on a Picanol Omni Plus
loom were replaced with those having 16 holes to obtain further reduction in
air consumption as suggested by the manufacturing company (Figure 6). All other
machine and fabric parameters were kept the same.
Loom and fabric parameters:
Loom and fabric parameters Dornier LW air-jet m/c Picanol Omni Plus air-jet m/c
|
Running speed (rpm).
650 830
|
Reed width (cm)
205 235
|
Reed number
130/2 130/2
|
Number of relay nozzles 28
35
|
Fabric construction
Plain weave (1/1) Plain weave (1/1)
|
Warp yarn
Ne 30/1 (20 tex) OE-rotor Ne 30/1 (20 tex) OE-rotor
|
Weft yarn
Ne 30/1 (20 tex)
OE-rotor Ne 30/1 (20 tex) OE-rotor
|
Number of warps
5346
6126
|
Warp density (warp/cm). 26
26
|
Weft density (weft/cm) 26
26
|
Effect of relay nozzle diameter
change in air consumption and loom efficiency by using
smaller a relay nozzle hole diameter.
Diameter of relay nozzle (mm)
|
1.4
|
1
|
Air consumption in m3/h/loom
|
63
|
50
|
Loom efficiency in percentage
|
95.4
|
96.1
|
Reduction in air consumption per relay nozzle ( m3/h)
|
0.4643
|
In the first part of the work, previously used relay nozzles with
1.4 mm hole diameter were replaced with the relay nozzles of 1 mm hole
diameter. The reason for selection of the relay nozzles with 1 mm diameter was
that they werethe only available nozzle diameters in the weaving mill during
the study. With this replacement, air consumption was reduced by 21% while a
slight increase in loom efficiency,which is the ratio of net loom running time
to the total time spent for production, was obtained, as can be seen in zles
with 1 mm diameter. Therefore, it is recommended that the minimum possible
relay nozzle diameter that is suitable for the filling yarn linear density used
is determined.
Effect of relay nozzle
blowing
In this part of the work, a truly experimental study was
con-ducted to optimize the blowing times on Picanol looms.Firstly, the average
increase in air consumption with the icrease of blowing time was determined as
shown in . Then the minimum blowing time that enables both problem-free weaving
and the same loom efficiency level to be maintained was determined.
Deterermination of average increase in air consumption with
blowing time.
Blowing time of relay
nozzel (In degrees)
|
Air consumption
(m3/h)
|
The increase in air
consumption per degree
(m3/h)
|
55
|
75
|
-
|
60
|
78
|
0.6
|
65
|
82
|
0.8
|
70
|
84
|
0.4
|
75
|
87
|
0.6
|
80
|
90
|
0.6
|
85
|
93
|
0.6
|
90
|
95
|
0.4
|
95
|
98
|
0.8
|
100
|
102
|
0.6
|
Avg
|
0.6
|
Measured air consumption values for different relay nozzle blowing
time adjustments.
Date
|
Relay blowing time (in
degrees)
|
Loom efficiency (%)
|
Saving in air
consumption (m3
/h/loom)
|
2/6/16
|
99.2
|
98
|
0
|
6/6/16
|
76.2
|
97.3
|
15.96
|
10/6/16
|
55.3
|
97.8
|
26.34
|
14/6/16
|
66.3
|
97.7
|
24.32
|
18/6/16
|
65.4
|
98.3
|
21.36
|
Conclusion
An experimental work was conducted to reduce the air consumption
on air-jet looms in a weaving mill with 202 looms in total. Frstly, relay
nozzles with a hole diameter of 1.4 mm replaced those with 1.0 mm diameter on
the looms euipped with single-holed nozzles and 20% reduction in air
consumption was obtained. Secondly, blowing times were optimized on other make
of air-jet looms equipped with multi-holed relay nozzles and this reduced the
air consumption by 20%. As a result, 20% reduction in air consumption. umption
for both types of air-jet weaving machine used in this work was achieved. Thus,
the weaving mill was able to save approximately 1200 €/loom/year which meant a
total saving of 240,000 €/year from energy costs with almost no expense. For
further reduction in air consumption of looms wijth multi-holed relay nozzles,
19-holed relay nozzles were replaced with the new 16-holed ones as recommended
by the manufacturer, as a third attempt to reduce air consumption. However, no
additional reduction in air consumption was obtained contrary to
expectations. Finally,the effect of the different number of filling ends per
tucking in applied by the pneumatic
tuck-in device was investigated and no significant change in air consumption
was recorded. In conclusion, this study showed that weaving mills could obtain
considerable savings in energy costs by working with single-holed relay nozzles
having smaller hole diameter and by achieving the shortest possible blowing
time adjustments on air-jet looms equipped with multi-holed relay nozzles,
without any decrease in loom efficiency and performance.
References
1)Textile Reasearch Journal (SAGE PUBLICATION
Vol 78 (2008)
2) International Journal of Engineering Trends and Technology (IJETT)
2) International Journal of Engineering Trends and Technology (IJETT)
Vol 54 November 3 Dec 2017
3)Journal of Engineered fibers and fabrics vol 4 (2014)
4) Journal of Asian Scientific Reasearch (2017) Asian Economic s and social society
5) Institutional Engineering and Technology( IET) vol 3 Dec 2013 Green global foundation
3)Journal of Engineered fibers and fabrics vol 4 (2014)
4) Journal of Asian Scientific Reasearch (2017) Asian Economic s and social society
5) Institutional Engineering and Technology( IET) vol 3 Dec 2013 Green global foundation
3 Comments
Nice practical information regarding air jet loom.
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ReplyDeleteAmazing article.
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